Flexography
Flexographic printing uses a printing plate made of rubber, plastic, or some other
flexible material. Ink is applied to a raised image on the plate, which transfers the
image to the printing substrate. The fast-drying inks used in flexography make it ideal
for printing on materials like plastics and foils. This makes flexography the predominant
method used for printing flexible bags, wrappers, and similar forms of packaging. The soft
rubber plates are also well-suited to printing on thick, compressible surfaces such as
cardboard packaging. Inks used in flexography are usually either water-based or
solvent-based (Pferdehirt, 1993).
The print area or image consists of a raised surface, known as relief printing, that
can be inked and pressed onto the substrate. Non-image areas are below the printing
surface and do not reproduce (Price, 1994). Both sheet-fed presses and web presses are
used in flexographic printing. A diagram for flexographic printing is shown in Figure 9.
Figure 9. Principle of Flexography
All original text, pictures, and illustrations are photographed to convert them into
the proper positive or negative films to make the plate which reproduces the image on the
substrate. This step includes the use of photographic chemicals, paper, and film. The
plates are made photomechanically, using a flexible material such as plastic or rubber,
and coated with solutions to make certain areas insoluble in water. Wastewater from this
process may contain acids, alkalis, solvents, plate coatings, and developers. If using
metal plates, non-image areas are etched with an acid solution that result in high
concentrations of heavy metals in the waste water. If using rubber or plastic plates, no
metals are introduced into the waste water. Ink is applied to the image on the plate. From
the plate, ink is transferred directly to the substrate. Wastes associated with this
process are waste paper, waste ink, and cleaning solvents. Air emissions containing VOCs
from inks and cleaning solvents are important waste streams (Price, 1994).
Flexographic printing has considerable impact on the environment based on the use of
rubber and photopolymer plates, solvent-based inks, and hydrocarbon solvents, as well as a
broad range of substrates. Printers select and mix chemicals for a variety of prepress and
pressroom applications. Darkroom chemistry, platemaking, inks and solvents, and
maintenance all use chemicals to achieve the ultimate goal of transferring a quality image
to a substrate (Shapiro, 1993a).
The traditional flexographic operation has many large, open containers for inks and
solvents which are used in the printing process. These evaporate rapidly into the plant
and are emitted through the exhaust stacks. Process waters are discharged from darkrooms,
cleaning tanks and cooling systems. Water-based inks may result in cleanup wastes going to
sewers or septic tanks. Adhesives used in converting may also find their way into the
water discharges. These wastes may still be considered to be hazardous in some states
depending upon their composition. The state regulatory agency will be able to provide
guidance on this issue. The manufacture of engravings for rubber plates and photoploymer
plate processing introduce sources of air, water and hazardous wastes (Shapiro, 1993a).
Plate Preparation
Citrus-based solvents and other more acceptable solvents have replaced the traditional
chlorinated solvents available to plate shops and printers who make photopolymer plates.
Water-washable photopolymer platemaking systems are now on the market. These are usually
classified as nontoxic, noncarcinogenic, and noncorrosive (Thompson, 1994).
Photopolymer masters have been introduced for making rubber plates. The hard
photopolymer replaces the metal engraving. Laser-engraved rubber plates have also been
introduced and provide a chemical-free means of platemaking. Future improvements might be
in the area of reuse and recycling of photopolymer plates, trim scrap and polyester cover
sheets, and further packaging reduction/reuse (Thompson, 1994).
In-line platemaking systems are fully enclosed and have microprocessor-controlled
exposure with processor and dryer/light finisher units. Light finishing via UV sources
with advanced automation and computerized controls ensures accurate platemaking and
reduced operator handling. These systems work well with a solvent-reclamation unit
(Thompson, 1994).
Inks
Water-based inks have been used most broadly among flexographic printers, especially
when printing on paper substrates such as corrugated containers. The first large-scale
testing of water inks on film and foil substrates occurred in late 1979 and continued
throughout 1980. In general, flexographic printers made the switch before it was required.
Trials began with white ink, which represents the largest ink usage for the majority of
flexographic printers. Early problems included poor adhesion, poor wet rub properties, low
gloss, and reduced press speeds (Morris, 1986). The poor adhesion has been particularly
troublesome with frozen food packaging.
Water-based ink technology has improved to the point where it is in the mainstream of
film printing. The colors produced are more vibrant and crisp than their oil counterparts
(Price, 1994). Films need further development to tailor them for the wetting-out and
adhesion of water-based inks. Inking and drying systems need modifications to achieve more
effective transfer and drying of water-based inks. In addition, there is a need for
cleaning systems that will facilitate the removal of all ink components and extend the
life of anilox rolls and doctor blade systems (Shapiro, 1993b).
With water-based inks, the surface tension causes beading (ink that will not "lay
down") that produces sharp process dots with less tendency to bridge. Printers
capitalize on that by using ceramic anilox cylinders and plates that release the ink more
readily to the substrate. Good ink trapping insures good process printing. To accomplish
good dry trapping one must increase the negative pressure on the in-between driers to
accommodate the increased expansion of water compared to alcohol, i.e., increase warm air
movement. Enclosed ink systems and ink temperature control can reduce amine loss and
retain the color strength at the original viscosity. Water-based inks dry in a 3-step
process; water evaporates from the ink, amines must leave the ink for the ink to have
water resistance, and the polymer emulsion particles must join to create a film or network
in the dried ink film. Water inks are more stable in high humidity conditions and do not
suffer solvent loss and the resulting changes in viscosity that solvent inks do. To
maintain good process printing with water-based inks, it is necessary to prevent excessive
mechanical agitation, maintain suitable pH, keep temperatures below 110 oF,
refingerprint press using water inks, and change to ceramic anilox cylinders (Matthiesen,
1993).
A new class of water-dispersible polyester resins is finding application in water-borne
flexographic printing inks and overprint lacquers. Unlike other aqueous ink systems that
rely on relatively high acid resins for water dispersibility, the new polyesters require
no neutralizing agents, such as ammonia or amines, to maintain water dispersibility. The
need to balance ink pH on the press is thus unnecessary, and odor problems associated with
volatile amines are avoided. These polyester systems dry faster on the substrate, allowing
faster press speeds or lower oven temperatures, and they exhibit rewettability on the
press (cylinders, plates, anilox rolls). This is all made possible because the linear
aromatic polyesters contain sodiosulfo groups (Barton, 1991).
Achievements in doctor blade technology have resulted in high quality flexographic
printing and pollution prevention through controlled ink transfer from the ink container
to the substrate. The average two-roll system with its ink fountain, fountain roller and
anilox roll is a veritable open reservoir, exposing large quantities of solvents that are
readily evaporated. The chambered doctor blade halts this evaporation. Ink enters the
chamber from the reservoir or ink sump by a pump. The ink is held in the manifold area,
with a small area exposed to the anilox roll. A doctor blade is positioned to shear off
the excess ink as the anilox turns, returning all extra ink to the chamber. A second
plastic or metal blade retains the ink within the chamber. The chamber is sealed off
completely so that no ink goes beyond the width of the unit. Anilox roll technology has
advanced to accommodate the wear of the doctor blade. When cleaning anilox rolls, use
automated systems with ultrasonic or high-pressure, and liquid cleaning (versus
mechanical) to reduce damage to rolls or cells.
Chrome-plated rolls have been replaced by laser-engraved ceramic surfaces. The blades
now wear instead of the roller (Shapiro, 1993b).
By using the chambered doctor blade system and other related improvements, the fountain
and the ensuing solvent exposure and evaporation have been reduced. The only ink solvents
evaporating are those carried by the anilox roll to the printing plates and then to the
substrate. No matter what the press speed, the ink amount deposited using doctor blades
will be consistent. Laser-engraved ceramic rollers wear better with the doctor blade in
place. An innovative chamber blade system with automatic washing system (automatic blanket
cleaners and ink levelers) built into the unit solves problems of ink remnants and reduces
the amount of water previously used to clean the printing system (Price, 1994.) Some
continuing problems with the blade systems include end-seal leaks, inks spitting-up from
seals on impression drums, set up and cleaning time on chamber systems, and part corrosion
with water-based inks (Shapiro, 1993b).
Several new and innovative drying and curing technologies have been developed that
reduce energy costs and work well with new ink formulations (Wold, 1991). Infrared drying
uses electromagnetic radiation and high energy concentration. It requires moderate capital
cost, and has high operating costs; it is often used in conjunction with convection air
dryers to provide the sensible heating load to the coated web. Radio frequency uses high
frequency electrical energy to dry water and solvent based coatings using high energy
concentration. There are high capital costs and moderate operating costs.
Supplemental convection air dryers are sometimes used in conjunction with radio
frequency.
Refer to the general pollution prevention section.
Like flexography, letterpress uses a plate with a raised image on a metal or plastic
plate. Once the predominant printing method, today it is used primarily for printing
books, business cards, and advertising brochures. The use of letterpress continues to
decline dramatically with lithographic, gravure and flexography replacing what was once
done by this technique.
The three types of letterpresses in use today are the platen, flat-bed, and rotary
presses. On the platen press, the raised plate is locked on a flat surface. The substrate
is placed on another flat surface and pressed against the inked plate. The flat-bed
cylinder press prints as the substrate passes around an impression cylinder on its way
from the feed stack to the delivery stack. These presses are often very slow relative to
lithographic, flexographic or gravure presses. The most popular letterpress is the web-fed
rotary letterpress (US EPA, 1995).
Barton, K.R. 1991. Water-based inks based on a new class of polyester resins. Polymers,
Laminations & Coatings Conference. 1991.
Matthiesen, D. 1993. Water Based Inks: Techniques in process printing. TAPPI Second
Annual Converting Short Course. May 1993.
Morris, John. 1986. "Low Solvent Ink Technology: Where is it Now? Where is it
Headed?" FLEXO, April 1986, p. 52-57.
Pferdehirt, W.P. 1993. Case Study: Roll the presses but hold the wastes: P2 and the
printing industry. Pollution Prevention Review. Autumn 1993.
Price, R.L. 1994. Printing & publishing industry pollution prevention and
recycling.
Center for Hazardous Material Research (CHMR) 530-4296-000. 1994.
Shapiro, F. 1993a. High-quality flexo can be environmentally responsible. FLEXO
18(8):68-71.
Shapiro, F. 1993b. Pollution Prevention. Boxboard Containers. May 1993.
Thompson, D.F. 1994. Green flexo: Converter can create competitive edge. Paper, Film
& Foil Converter April 1994: 68-70.
Wold, J.L. 1991. Maintaining productivity with convection air dryers when switching
fromsolvent based to water based applications including between station C.I. flexo
presses. Polymers, Laminations & Coatings 1991: 305-313.
Barton, K.R. 1991. Water-based inks based on a new class of polyester resins. Polymers,
Laminations & Coatings Conference.
This paper reviews a new class of water-dispersible polyester resins used in gravure
and flexographic printing inks. The chemical nature and qualities of these new resins are
discussed.
Bassemir, R.W. and R. Krishnan. 1990. Practical applications of surface energy
measurements in flexography. FLEXO
This is a technical paper that deals with the surface science of printing. Surface
tension of inks, viscosity, bubble pressure, and other physical properties that affect
print quality are discussed.
Capristo, M.G. 1986. Water inks can offer compliance cost effiency, performance
quality. FLEXO.
This paper gives some general information and statistics on switching to water-based
inks and the progress that has been made in developing water-based printing processes.
Fleischman, M., F.W. Kirsch, and G.P. Looby. 1993. Waste minimization assessment for a
manufacturer of product carriers and printed labels. USEPA RREL Environmental Research
Brief. EPA/600/S-93/008.
This brief reports on an assessment at a plant manufacturing high density polyethylene
product carriers and printed polystyrene packaging labels. Most of the waste was generated
by the cleaning of printing presses and printing plates. Opportunities for minimizing
solvent waste were recommended.
Kirsch, F.W. and G.P. Looby. 1990. Waste minimization assessment for a manufacturer of
printed plastic bags. USEPA RREL Environmental Research Brief. EPA/600/M-90/017.
This is a report of an assessment at a plant manufacturing ~ 1.8 million lbs. of
printed plastic bags for snack foods annually. The lamination process waste could be
handled with an automatic adhesive/solvent mixing system.
Matthiesen, D. 1993. Water Based Inks: Techniques in process printing. TAPPI Second
Annual Converting Short Course. May 1993.
This paper provides a thorough overview of the physical properties of water-based inks
and how those properties affect print quality. Numerous recommendations are made on how to
maintain and improve print quality.
Parsons, R., B. Donovan, and M. Hayward. Ultrafiltration for the treatment of ink and
starch wastewater in the corrugated container industry.
This technical paper describes the use of ultrafiltration in treating flexographic ink
wash water and dilute starch adhesive waste.
Pferdehirt, W.P. 1993. Case Study: Roll the presses but hold the wastes: P2 and the
printing industry. Pollution Prevention Review, Autumn 1993.
A review of the printing industry, including a description of the basic printing
processes, is given. Waste reduction opportunities are explained, along with a review of
progress that has been made in pollution prevention in the printing industry.
Price, R.L. 1994. Printing & publishing industry pollution prevention and
recycling. Center for Hazardous Material Research (CHMR) 530-4296-000.
Student manual prepared for the Illinois Environmental Protection Agency. This manual
gives the history of the printing industry, and statistics about Illinois printing
establishments. Each of the printing processes are explained and diagramed. The common
pollution prevention and waste reduction opportunities are explained.
Shapiro, F. 1993. High-quality flexo can be environmentally responsible. FLEXO
18(8):68-71. The effects of environmental legislation and resulting compliance on the
printing industry is discussed.
Shapiro, F. Impact of hazardous waste on the package printer/converter. FLEXO
Wastes generated at each step of the printing process are described, along with ways to
minimize those wastes.
Shapiro, F. 1993. Pollution Prevention. Boxboard Containers. May 1993.
Pollution prevention and waste reduction in the boxboard industry are discussed in
relation to compliance with regulations and quality manufacturing.
Shields, G.N. 1994. New method to clean anilox rools. FLEXO 19(4):36-40.
Automated cleaning systems with multiple-nozzle spray bars, and liquid-through-liquid
spray cleaning are discussed.
Strutt, D.B. 1991. Photopolymers achieve new quality levels in flexographic printing.
Polymers, Laminations & Coatings 1991: 337-338.
The use of photopolymer printing plates and their impact on quality and printing speed
are discussed.
Thompson, D.F. 1994. Green flexo: Converter can create competitive edge. Paper, Film
& Foil Converter April 1994: 68-70.
A brief overview of P2 and waste reduction opportunities in flexographic printing.
Wold, J.L. 1991. Maintaining productivity with convection air dryers when switching
from solvent based to water based applications including between station C.I. flexo
presses. Polymers, Laminations & Coatings 1991: 305-313.
Drying/curing technologies are reviewed. The technical aspects of drying, including
heat transfer and evaporation rates, are presented along with actual data from test drying
stations.
Related industries
Hang, M. 1994. Alternative Plate Processing. FLEXO 19(1): 50-52.
This article compares closed-loop solvent plate systems with water-washable plate
systems as alternatives to perchloroethylene washout solutions.
Mounsey, G. 1994. Alternative Washout Solutions. FLEXO 19(4): 31.
The hazards of perc/butyl washout solutions and the benefits of alternative washout
solutions are discussed.
Case Study 1
Replacement of Hazardous Material in Wide Web Flexographic Printing Process
Kranz, P.B., T.R. Williamson,and P.M. Randall
USEPA RREL Project Summary. EPA/600/SR-93/149. 1993.
A wide web flexographic printing firm substituted water-based inks for solvent-based
inks when manufacturing flexible packaging using plastic sheet substrates (e.g., plastic
bags for bread). The project objectives were to evaluate the technical feasibility,
economic effect, and resulting change in VOC emissions achieved by the substitution. The
technical evaluation was to quantify the reduction in both volatile and liquid-phase solid
hazardous wastes. Reduction of VOC emissions by switching from the use of solvent-based
inks to water-based inks required several equipment modifications and a feedstock
substitution, including dryer capacity enhancement, press roller modification, ink
handling equipment upgrade and installation of an in-line corona treatment system.
Water-based inks containing 72.5 percent less VOC were used in place of, and combined
with, traditional solvent-based inks.
For each percent increase in water-based ink use, VOC emissions were reduced 14 lb.
This was based on usage of ~2250 lb. of solvent-based ink per week, resulting in VOC
emissions of about 1570 lb. Typically the substitution did not adversely affect product
quality or non-hazardous scrap waste generation. An average reduction of 95 percent of
liquid F003 waste from waste ink and cleaning solvents resulted from operational practice
changes and employee training.
The economic evaluation was completed by calculating the costs of press modifications,
ancillary equipment, waste disposal, inks, and solvent. The project had a positive net
present value of $39,165 and a payback period of 2.5 yr, based on 21 percent utilization
of water-based ink; 100 percent utilization of water-based inks would yield a payback
period of 0.54 yr.
Additional benefits from reduced VOC emissions and liquid hazardous waste have been
improvements in the workplace resulting from the switch to water-based inks include
reduced indoor air pollutants, reduced handling of hazardous solvents, and the
appreciation by company employees of the need to make a conscious effort to further reduce
waste generation. |
Case Study 2
Achievements in Source Reduction and Recycling for Ten Industries in the
United States
J. W. Tillman
USEPA RREL Report. EPA/600/2-91/051. 1991
Amko Plastics, Inc., in Cincinnati, Ohio is a decorative printer for packaging of
consumer products, retail store packaging and industrial packaging employing approximately
280 people. By switching from solvent-based inks to water-based inks, they have minimized
their volatile emissions by an estimated 88 percent. The reduction of alcohol solvent
vapors has improved the ambient air quality of the press room.
The following process changes and modifications were evaluated and implemented:
- Control of pH of the ink to maintain viscosity and print quality.
- Modification of dryer heads between successive color print stations to direct heated air
onto the printed film (increased drying capability for water-based inks).
- Redesign of ink metering systems for handling a higher strength ink and thinner
application.
- Replace metal anilox rolls, which were having their wear-life drastically reduced, with
more expensive ceramic rolls.
- Switch the fountain roll surface material to a harder durometer rubber to improve
wear-life with ceramic anilox rolls.
- Develop systems and equipment to inversely vary the percentage of resin `slip additive'
blended into the resin as the film was being extruded to allow high speed printing.
- Installation of larger corona treating systems for electrostatic treatment of the film
surface at the higher surface tension required for water-based inks.
- Switch to foam cushion `sticky-back' from conventional `sticky-back' to compensate for
the additional pressure needed with water-based inks to achieve impression.
The major costs incurred by Amko from 1984 to 1987 (exceeding $2 million) have today
resulted in the ability to print with quality and productivity at the same level as U.S.
solvent-based printers. |
Case Study 3
Solvent Recovery from Flexographic Printing Inks
D.C. Crump
Pollution Prevention: Proceedings for the Conference "Waste Reduction - Pollution
Prevention Progress and Prospects within North Carolina. Ed. Gray, et.al.
Rexham Corporation installed a two-stage distilling process at their flexographic
printing plant in Greensboro to recycle used solvent. A special room was built to house
the stills and all appropriate safety features were incorporated. They have found that
uncut ink cannot be distilled due to charring. This onsite distillation has reduced the
amount of hazardous waste to a level that changed the status of the generator to small
generator. |
Case Study 4
Venture Packaging, Charlotte NC.
Case Summaries of Waste Reduction by Industries in the Southeast
Waste Reduction Resource Center for the Southeast, Raleigh, NC, 1989
Venture Packaging undertook a project to replace solvent-based inks, coatings and
adhesives with water-based materials to reduce emissions and the volume of ignitable waste
generated. Since implementing this program in 1980, emissions have been reduced by
approximately 55 percent. An additional 15 to 20 percent reduction appears possible with
further application of water-based materials. The greatest success has been achieved in
adhesives. Water-based adhesives are now being used for almost all production. Ink
development has been more difficult and has varied with the substrate to be printed.
Laminating inks have been more successful than surface-print inks.
Capital expenditures have been minimal, but experimental costs have been incurred. The
alternative, the addition of incineration equipment, would be very costly. |
Case Study 5
Water and Ink Waste Reduction at F.C. Meyer Company
Toxics Use Reduction Case Study
Massachusetts Office of Technical Assistance -C101-2, 8/93
F.C. Meyer Company, a Lawrence, Massachusetts cardboard box manufacturer and printer,
employs 200 people operating eight printing presses over three shifts/day, five days/wk.
In 1989, F.C. Meyer switched from solvent-based inks to water-based inks, and reduced its
VOC emissions from 280 tons per year to less than 1,000 lbs.. per year. Performance
quality was unchanged and the regulatory workload was reduced substantially. In 1992 they
began to seek further waste reduction opportunities in the area of press cleaning
procedures. Through employee training, and improved washing practices, the company was
able to reduce wastes from 10 drums of hazardous waste to 2 drums of nonhazardous waste
per week. This reduction was achieved by draining and scraping as much ink as possible
before washing, and minimizing the amount of water used.
In addition to reducing the volume of wash water used, the company asked its supplier
to deliver black ink with 10 percent reduced water content. Waste water was added to the
black ink with no apparent effect on the color quality of the ink. The waste water can
also be added to other colors, such as gray, in smaller amounts than when added to black
ink.
Reductions achieved
Solids in spent wash water were reduced from more than 30 percent to 13 percent. The
volume of water used decreased by 35 percent; about one pint of water is now used each
time a press is washed. By reusing most of the wash water, waste disposal has decreased
from 10 to 2 55-gallon drums per week. The 55-gallon drums of waste cost ~$100 each to
dispose. Implementing the reuse of ink waste water has reduced the yearly cost of waste
disposal from $52,000 to $5,200. |
Case Study 6
VOC Reduction at Hampden Papers, Inc.
Toxics Use Reduction Case Study, C201-1, 8/93
Massachusetts Office of Technical Assistance
Hampden Papers Inc. of Holyoke, MA, reduced emissions of VOCs by 97 percent over a ten
year period by using new aqueous based acrylics developed by I.C.I. Resins US of
Wilmington, MA. Hampden is a 180-worker specialty manufacturer of converted paper, film,
foils, and boards with 64 production lines in a 300,000 ft2 facility. In the
1970s they elected to pursue reduction at the source rather than emission control. The
company implemented a new coating system using non- and low-VOC inks and coatings and now
uses gas oven drying and electron beam curing where necessary. They have not had to
purchase VOC collection and control equipment.
Hampden found that I.C.I. acrylic copolymer resin inks and coatings have fast drying
characteristics. Thermally sensitive films and coatings are cured in one of the first
Energy Sciences electron beam units ever installed. Infrared technology is also used to
improve drying. The aqueous products have demonstrated excellent clarity and resolubility
on the press.
Over a 10-year period, Hampden has reduced annual VOC emissions at its facility by 97
percent, from over 420 tons to less than 20 tons. VOCs emitted per unit of product dropped
from 8.15 pounds to 0.22 pounds. Hampden increased total production by 21 percent in the
same period and has realized significant savings in fire insurance premiums. The reduction
of VOCs has resulted in lower compliance costs, savings on insurance premiums, and a safer
work environment. |
Case Study 7
A (UV) Cure That's Eco-Friendly
Graphic Arts Monthly, November 1991:S6
James River is a marketer and manufacturer of consumer products, food and consumer
packaging, and consumer-related communications papers. Their product lines include brands
such as Northern bathroom tissue, Brawney paper towels, Dixie cups and plates, Monterey
magazine paper, and the Quilt-Rap sandwich wrap. Sales for 1990 were $5.4 billion.
In 1975 James River began using UV-cured inks, and by the mid-1980s a significant
process expansion was undertaken. UV-cured inks are used in the converting process. They
create the opportunity to combine multiple steps into an in-line process. These inks dry
instantly and are more energy efficient, but generally cost more than conventional inks. |
Case Study 8
Tubed Products, Inc. Use Reduction Case Study
Office of Technical Assistance, Commonwealth of Massachusetts
Case Study No. 31. Nov. 1995
Tubed Products, Inc., of Easthampton, MA is a manufacturer of plastic squeeze tubes and
caps for the cosmetic, personal care, pharmaceutical, and household chemical market. About
40 percent of their production is decoration of tubes with specific logos and information
specified by customers.
Tubed Products made the switch to ultraviolet inks and coatings over a period of 20
years. Trials with their first UV decorating line in the early 1970s showed that UV
systems had significantly reduced emissions, required less energy and floor space, reduced
waste ink (since UV inks do not dry on the press), and allowed them to blend base inks to
achieve custom colors. In 1979, after working with coating manufacturers to develop and
evaluate UV-curable tube coatings, they purchased their first production line that used UV
curing for both inks and coatings. Later, `on-mandrel' UV curing equipment was designed
and manufactured that allowed tubes to be printed, coated, and capped while mounted on the
same mandrel, thereby eliminating the need for tube transfer mechanisms.
Conversion to UV-cured inks and coatings required new procedures for color matching,
measurement of surface friction, permeation, flexibility, and non-yellowing properties.
The addition of high speed presses and UV lamp systems required additional training.
The benefits of switching to UV curing have been space and energy savings; each line
occupies about one-third the floor space of a comparable thermal line and about one-fifth
the energy (12,000 watts per hour). Thermal lines need about 40 minutes to produce a tube,
while the high-speed on-mandrel lines take only 5 minutes. UV inks and coatings contain no
solvents, reducing worker exposure and environmental concerns significantly. Although the
firm has not calculated the exact cost savings, they believe that switching to UV systems
has been an important factor contributing to its growth in the industry, helping it to
become a low-cost producer and the largest US supplier of plastic squeeze tubes. |
Case Study 9
How We Anticipated and Corrected Problems When Converting to Water
F. Lamar Jones, Label America, Inc.
Flexo, July 1990
In the beginning, all press operators were very experienced, but only with
solvent-based inks. During the transition from solvent- to water-based inks, customers
were demanding better color matches, more consistency from run to run, and much improved
light-fastness. Suppliers were not providing inks that were base color consistent, and
service was poor. Other flexo converters were beginning to switch to water inks, so we
looked for a supplier that would commit to us, providing both service and quality, and
made the switch.
We chose one press and one pressman to experiment with the water-based inks. That
minimizes disruption in the pressroom, and allowed us to "work off" the
inventory of solvent-base inks. We had to make adjustments in press speed, wash-up sink,
substrates, tools, and ink additives.
Press speed: We routinely run water-based inks at 400-500 feet per
minute, on both gloss and uncoated stocks. We have found that movement of air is as
important, if not more important, than heat, in the drying of water-based inks.
Wash-up: Water-based inks require a mild soap solution for wash-up. In
order to avoid contamination of the inks with this solution, a custom wash-up sink was
built. It is centrally located in the pressroom and large enough to accommodate the ink
pan, bucket and pump. At the end of the job, ink is drained back into the ink container.
Residual ink in the pan, bucket, and pump go to the sink where the wash solution
circulates through until they are clean (about 3 minutes). Disposable pans are available,
which would also reduce wash-up time.
Substrates - paper vs. film: Label America, Inc. specializes in EDP
labels, both pinfed and sheetfed, so the bulk of the printing is on uncoated paper, which
may be rough. Ink coverage can be improved with ink additives. Our experience has been
that with proper primer and specially formulated inks, we can effectively print on films
and foils with excellent results.
Tools: With the switch to water-based inks, we had to make more use of
Zahn cups and pH meters to maintain the ink quality.
Ink maintenance: Replenishment is added as needed, and the pH meter is
used often.
Ink additives: Slow, medium, and fast dry reducer, print cleaning
additive, glycol, ammonia, extender and color boosters are all being used to improve print
quality
Computerized ink mixing: This is among the most significant changes
for Label America, Inc. It has paid for itself several times over within a year. It has
reduced raw material purchases by allowing the company to purchase only base colors. It
allows for effective mixing of even very small batches, reduces mixing time to about 3-4
minutes, and allows us to keep much better record of ink inventory.
Water-based inks are better environmentally and for human health - (fire hazard,
solvent fumes, ease of disposal.) Inventory has been reduced by over half and sales have
doubled. Insurance costs have decreased. Color consistency and colorfast characteristics
have improved. |
Case Study 10
The Spirit of Innovation
Martha Ortmann
Boxboard Containers, pg. 32-33
Lawrence Paper decided to retrofit its printing stations with a new, more efficient
doctor blade system. The original open system was too costly in terms of ink consumption
and contamination. Printco is a company that does retrofittings on printing presses. The
retrofit involved many weeks working with the intricacies of the press, and engineering
and redesigning the plate system. The new system saves ink and improves print quality. The
blades are changed more often, and blade pressure is determined and adjusted
automatically. Laser engraved anilox rolls are used as opposed to mechanically engraved
ones.
Advantages of the new system: the old system used 30 to 40 lbs. of ink per ink change
whereas the new system requires only 8 lbs. which reduces ink usage and volume of ink
contaminated; blades can now be changed in 20 minutes versus an hour with the old system;
the new system is detachable, making repairs easier.
Lawrence Paper recycles 100 percent of the water used in the printing process. |
Case Study 11
Waste Minimization Assessment for a Manufacturer of Product Carriers and
Printed Labels
Waste Minimization and Recycling Report, 1994
Government Institutes, Inc.
A plant manufacturing printed polystyrene packaging labels and high density
polyethylene (HDPE) product carriers with over 400 employees produces 8 billion labels and
over 500 million product carriers each year.
Wastes produced include volatile emissions (from the polystyrene extrusion process from
the blowing agent Freon-22TM and impurities in the polystyrene); photoprocessing wastes;
plate washing wastes (butanol/perchloroethylene solvent mixture), both liquid and volatile
emissions; damaged or obsolete plates; solvent inks; press washing solvents (liquid and
volatile emissions); defective product; wastes from the thermoforming and cutting process.
Solvents are recovered with two large distillation units and reused in the plant; all
extrusion wastes that have not been inked are reground and reworked onsite; off-spec inks
and surplus inks are reworked; ink runs are scheduled to allow light-to-dark transitions
in the printing trays; wash-up solvent is recovered onsite for reuse.
The economic savings from the waste minimization opportunities implemented result from
the need for less raw material and from reduced waste treatment and disposal. Additional
waste minimization opportunities are listed in the case study. |
Case Study 12
Thinking Positive about Compliance Pollution Prevention through Process
Improvement
Fred Shapiro
Polymers, Laminations & Coatings Conference: 315-320
1991
A flexographic printer of stationery items and coating paperboard with overall solid
colors was concerned with disposing of wastewater. Corporate engineers estimated the
volume at 50 gallons per day, but further inspection revealed that one press operation
alone was generating about 1,000 gallons per week. Examination of the printing process
also revealed poor scheduling, untrained personnel, unsound practices in sequencing of
colors, inadequate accessory equipment to facilitate efficient changes of color, and using
free running water to clean parts during changes. A wastewater treatment unit was
installed at a cost of $40,000 - $50,000.
Added ink pans and ink pumps helped make color changes more efficient. A cleaning tank
was purchased so parts could be cleaned while the press was running, reducing the length
of time it took to change colors and the amount of water used. Improved scheduling of
colors eliminated some of the cleanup as well. Savings in downtime alone amounted to over
$100,000 per year. |
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